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Old Dec 6, 2010 | 10:01 AM
  #1651  
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I will be going to the shop after work to have the BNR's actuator adjusted. Should be fairly obvious if the the adjustments work
Old Dec 6, 2010 | 10:14 AM
  #1652  
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Originally Posted by pdxhak
I will be going to the shop after work to have the BNR's actuator adjusted. Should be fairly obvious if the the adjustments work
Hopefully the adjustments make a world of difference. Good luck!
Old Dec 6, 2010 | 10:16 AM
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Good luck man!!!!
Old Dec 6, 2010 | 10:52 AM
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good luck pdx. let me know how it goes!
Old Dec 6, 2010 | 11:28 AM
  #1655  
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Thanks guys. I'm hopeful it will make some form of a difference. I'm trying not to get my hopes up so I will not be disappointed. I will data log regardless. If the adjustments are fairly positive then I will put the car back on the dyno just to see the numbers before MM does his final tune on 12/17 with Surgeline.
Old Dec 6, 2010 | 01:42 PM
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Originally Posted by J.Cab
I will take a look one day when I take my turbo kit off so that I can sell it. It is definitely odd that I am on the stock Greddy actuator and am able to hold the boost. I will say that Bryan did modify my wastegate, so its not the prettiest actuator out there (it had been cut open, etc.) It had some work done to it, now as to what he did I do not know. But I was very pleased with the performance of it.
If it's been cut open , my guess is that a bigger spring has been fitted . And It was probably done by a previous owner as Bryan has never mentioned doing that kind of thing .
Old Dec 6, 2010 | 02:36 PM
  #1657  
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Originally Posted by Brettus
If it's been cut open , my guess is that a bigger spring has been fitted . And It was probably done by a previous owner as Bryan has never mentioned doing that kind of thing .
Doubt it. Without the boost controller, I was right at 6-7 psi on just the actuator.

Last edited by J.Cab; Dec 6, 2010 at 04:41 PM.
Old Dec 6, 2010 | 02:38 PM
  #1658  
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Originally Posted by J.Cab
Doubt it. Without the boost controller, I was right at 6-7 psi on just the wastegate.
which is 2psi higher than a stock greddy (with the fix#2 done)
Old Dec 6, 2010 | 03:21 PM
  #1659  
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Originally Posted by Brettus
If it's been cut open , my guess is that a bigger spring has been fitted . And It was probably done by a previous owner as Bryan has never mentioned doing that kind of thing .
https://www.rx8club.com/showpost.php...6&postcount=29

I was going to post a picture of the actuator when I unistalled the turbo kit, but I will respect Bryan in this matter.

Last edited by J.Cab; Dec 6, 2010 at 04:41 PM.
Old Dec 6, 2010 | 04:16 PM
  #1660  
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Originally Posted by J.Cab
https://www.rx8club.com/showpost.php...6&postcount=29

I was going to post a picture of the wastegate when I unistalled the turbo kit, but I will respect Bryan in this matter.
could not see anything in that post mentioning the actuator ?
Old Dec 6, 2010 | 04:43 PM
  #1661  
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Originally Posted by Brettus
could not see anything in that post mentioning the actuator ?
Well I will say this much, the actuator definitely has some work done to it. I will let Bryan elaborate more on it!
Old Dec 6, 2010 | 05:30 PM
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Originally Posted by J.Cab
Well I will say this much, the actuator definitely has some work done to it. I will let Bryan elaborate more on it!
The concept has been discussed at some length before BTW and I do know a guy here in NZ who has had this mod done done by a very experienced turbo builder .
That turbo has still not been fitted so don't know the outcome but I will say that my experimentation with a helper spring (attached to the side of the actuator)achieved similar results to what you got .
Old Dec 6, 2010 | 10:42 PM
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The plot thickens! LOL

I could imagine a bigger spring being a good way to solve this (to a degree). Still allows for complete movement, but at the same time raises cracking pressure.
Old Dec 6, 2010 | 10:50 PM
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The adjusted actuator is holding boost. We did a few runs in 2nd and 3rd gear to 8k and 8.5k and it was holding. We think we saw 12-13 psi at 8k and 8.5k dropped just a tad under 10 psi. The boost controller turned off as well. Next up is some data logging
Old Dec 6, 2010 | 10:59 PM
  #1665  
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Originally Posted by pdxhak
The adjusted actuator is holding boost. We did a few runs in 2nd and 3rd gear to 8k and 8.5k and it was holding. We think we saw 12-13 psi at 8k and 8.5k dropped just a tad under 10 psi. The boost controller turned off as well. Next up is some data logging
wow - so that was all that was done ? Looks like I spoke too soon ....

beeter get that beast back on the dyno then
Old Dec 6, 2010 | 11:00 PM
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Yep! The actuator was adjusted about 1/2". I believe Marc said about 2 or 3 threads left.
Old Dec 6, 2010 | 11:01 PM
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I need to read up on how to use the AP so I can data log and post up the info. I want to see the data and not just rely on the gauges.
Old Dec 6, 2010 | 11:01 PM
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12-13 psi on just the gate..... errr, might want to think about loosening that up some.

Very cool to hear it is fixed; but I can see that ending badly LOL!!!!!
Old Dec 6, 2010 | 11:06 PM
  #1669  
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The shop said the same thing. They wanted to tune the BC but I requested they leave it alone until Jeff is done with his tune. We will probably back it down and then use the BC.
Old Dec 6, 2010 | 11:14 PM
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don't forget what we talked about . Just getting that boost is no garantee you are making the power you should be making .

Unless it feels like godzilla already ? In which case ignore everything i've said LOL
Old Dec 6, 2010 | 11:19 PM
  #1671  
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The car is definitely pulling harder. Boost comes on fast and seems to pull strong to 8k. Again I do not want to reply on feel or the gauges. I will log data and post it up so we can all see what is happening
Old Dec 6, 2010 | 11:24 PM
  #1672  
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if you want to test it against other cars and see where you are at before you go to the dyno check out this thread :

https://www.rx8club.com/series-i-major-horsepower-upgrades-93/dudelogger-internet-racing-challenge-173494/
Old Dec 7, 2010 | 02:04 AM
  #1673  
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glad to hear its holding, pdxhak. definitely get some logs of your maf readings. if you have any of the logs left on the ap from when jeff dynotuned it, it'd be a good comparison.
Old Dec 7, 2010 | 04:42 PM
  #1674  
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The alternator went and the harness melted a bit on the way to work. Hopefully this did not cause any issues with the motor. The car had to be towed home because other systems in the car would not function.

Old Dec 7, 2010 | 04:46 PM
  #1675  
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/\ nut not tightened up properly ?

damn - that sucks

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