9krpmrx8's Boost Build Thread
#1676
No respecter of malarkey
iTrader: (25)
Change of plans.
I just spoke with a tech at ATP and he broke it down for me an basically told me that it is due to excessive crankcase pressure and that I need to properly diagnose the issue before I start adding restrictors. So I will fit a different catch can tonight and then I need to measure the pressure of the oil that the oil feed line is seeing.
Check out what he said
I just spoke with a tech at ATP and he broke it down for me an basically told me that it is due to excessive crankcase pressure and that I need to properly diagnose the issue before I start adding restrictors. So I will fit a different catch can tonight and then I need to measure the pressure of the oil that the oil feed line is seeing.
Check out what he said
Except that doesn't make any sense if you have a scavenge pump and it is both plumbed and operating properly. You did tell him you have this, right?
#1677
SPOOLN8
iTrader: (1)
Join Date: Nov 2008
Location: Edmonton, Alberta, Canada
Posts: 2,225
Received 208 Likes
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Yeah man you are completely over worrying this..... brand new engine is gonna smoke... no matter what engine it is. And how many people have you heard of witha scavenger pump on a greddy turbo.... I doubt you will need a restrictor
#1678
Boosted Kiwi
iTrader: (2)
I am running a scavenge pump due to the position of the oil drain on the particular center section I am using, because it does not sit straight up and down. I doubled checked the flow direction of the pump and it is correct and is sucking oil out of the turbo and pushing it down to the pan and I am using standard oil drain return line so the hose is plenty big enough. I think bumblebeerx8 is right and that I need a check valve on the return side. I will pick one up today.
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#1679
SPOOLN8
iTrader: (1)
Join Date: Nov 2008
Location: Edmonton, Alberta, Canada
Posts: 2,225
Received 208 Likes
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^ hehe... and besides 9k, if you blow a turbo than you can custom mount a flange to a garret BB and let me know how it goes so I don't have to lead the way on this one.... of coarse all behind Jeff but you know what I mean :D
#1681
SARX Legend
Thread Starter
iTrader: (46)
The car is running fine now and my scavenge pump is working perfectly I don't need the restrictor, the addition of the check valve and routing the breather hose at the filler neck to the intake fixed it. I have to run the scavenge pump because the drain is at an angle so I don't have much gravity to help me. The scavenge pump is setup and ran with a check valve that cracks at .5 PSI, this way I don't have to worry about oil backing up into the turbo.
The smoke went away after about 45 minutes I ditched the catch can and routed the hose to the intake and extended the MAF wiring.
I lengthened the MAF wiring and everything seems to be good. I did get a code for a stuck APV but I reset the ECU and it went away. I will have my son help me put the hood back on tomorrow (no help today to do it) and finish up my gauges and some other electrical stuff this weekend and then I will load Kane's base tune and data log.
The smoke went away after about 45 minutes I ditched the catch can and routed the hose to the intake and extended the MAF wiring.
I lengthened the MAF wiring and everything seems to be good. I did get a code for a stuck APV but I reset the ECU and it went away. I will have my son help me put the hood back on tomorrow (no help today to do it) and finish up my gauges and some other electrical stuff this weekend and then I will load Kane's base tune and data log.
Last edited by 9krpmrx8; 12-02-2011 at 12:53 AM.
#1682
WENTGERMAN
iTrader: (6)
The car is running fine now and my scavenge pump is working perfectly I don't need the restrictor, the addition of the check valve and routing the breather hose at the filler neck to the intake fixed it. I have to run the scavenge pump because the drain is at an angle so I don't have much gravity to help me. The scavenge pump is setup and ran with a check valve that cracks at .5 PSI, this way I don't have to worry about oil backing up into the turbo.
The smoke went away after about 45 minutes I ditched the catch can and routed the hose to the intake and extended the MAF wiring.
I lengthened the MAF wiring and everything seems to be good. I did get a code for a stuck APV but I reset the ECU and it went away. I will have my son help me put the hood back on tomorrow (no help today to do it) and finish up my gauges and some other electrical stuff this weekend and then I will load Kane's base tune and data log.
The smoke went away after about 45 minutes I ditched the catch can and routed the hose to the intake and extended the MAF wiring.
I lengthened the MAF wiring and everything seems to be good. I did get a code for a stuck APV but I reset the ECU and it went away. I will have my son help me put the hood back on tomorrow (no help today to do it) and finish up my gauges and some other electrical stuff this weekend and then I will load Kane's base tune and data log.
#1690
Yeah, an exhaust fan would be good...
Glad to hear she's done and in excellent shape. Wish I had the fuzzies (and know how) to take on a build like this.
For now I'll just have to read the cool threads.
Glad to hear she's done and in excellent shape. Wish I had the fuzzies (and know how) to take on a build like this.
For now I'll just have to read the cool threads.
#1691
SARX Legend
Thread Starter
iTrader: (46)
I have done a few engine swaps/turbo installs in my lifetime and this was by far the most time consuming. But mainly because it was on a car with 127,000 miles so I had to fix and replace a ton of stuff.
once my car is completely finished I will start a new thread that summarizes my experience. But basically there are a few lessons learned and as usual I made things harder than they needed to be but hopefully those decisions pay off in performance. I am expecting to put down some pretty good numbers, we will see.
once my car is completely finished I will start a new thread that summarizes my experience. But basically there are a few lessons learned and as usual I made things harder than they needed to be but hopefully those decisions pay off in performance. I am expecting to put down some pretty good numbers, we will see.
#1696
SARX Legend
Thread Starter
iTrader: (46)
here is a short vid I took at 2am in the dark with my cell phone If you have a seizure watching it I am not responsible. I started it again after resetting the computer and the misfire codes and APV codes went away. Not sure what was going, I think she just needs to be driven.
Last edited by 9krpmrx8; 12-02-2011 at 11:34 AM.