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Dyno Day for REAL with MM in Portland

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Old 12-06-2010, 09:14 PM
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Originally Posted by dondo
well mine wont read properly right cause it was pegging the maf and reporting 500g/s?
careful, that could open a wormhole if u mat it...
Old 12-06-2010, 09:25 PM
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Originally Posted by Nemesis8
your killing me dude - lolz

lowering springs are in your future
I just want to feel cool like you!!
Old 12-06-2010, 10:04 PM
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Stopped by FD3S after work. Marc threw the car up on the lift and adjusted the actuator about 1/2" I think. He said there are just a few threads left to turn. Anyway the car is holding boost! Adam (Marc's shop manager) went for a ride with me and he was monitoring the boost gauge and boost controller (zeroed out) and we saw 12 - 13 psi on 2nd and 3rd gear pulls. I think around 8500 RPM boost dropped just below 10 psi. I will data log tomorrow and upload the data so everyone can look it over.

BOOOOOST
Old 12-06-2010, 10:44 PM
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Congrats!!!
Old 12-06-2010, 10:51 PM
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Thanks man! It feels so much better! Really looking forward to finishing up the tune on 12/17.
Old 12-06-2010, 11:46 PM
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awesome man - can't wait to hear the results!
Old 12-07-2010, 12:02 AM
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At least the RAW un-smoothed charts, show better resolution for AFR and Boost curves. So does that makes them relevant?
Old 12-08-2010, 12:54 PM
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Originally Posted by dondo
can you email me all the 8 pulls? the guy never sent me any.

thanks!

Got all six runs for your car. I can forward them tonight.
Old 12-08-2010, 05:47 PM
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The gauge pod I order has horrible fitment. I sent a PM to evo-r to see what they can do about it. Also have an alternator and wiring harness coming. Yes yes lots of work on the car Still keeping my fingers crossed the motor did not go belly up. Not sure if I will be ready by next Friday for the final tune with MM. If I still have issues by Wednesday then I will reschedule.
Old 12-08-2010, 06:00 PM
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I talked to Cam today and he says that bypass valve should be open during vacuum/cruising and as soon as you get on the throttle and build boost it should shut and not open again.

Since the dyno showed the boost fluctuation at 6k he thinks something is up with that valve so I'll have to investigate a bit. He also said I should be making way more boost than 9psi and who should be over 300whp.

It's located within reach so hopefully I can figure it out..
Old 12-08-2010, 07:31 PM
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Originally Posted by pdxhak
Still keeping my fingers crossed the motor did not go belly up. Not sure if I will be ready by next Friday for the final tune with MM. If I still have issues by Wednesday then I will reschedule.
What happened to your motor???
Old 12-08-2010, 07:43 PM
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The alternator crapped out while I was full throttle. I heard 3 quick pops. Not a loud crack sound and do not think it was back fire. The previous night FD3S adjusted the actuator and was able to hold boost with the BC zeroed out. Car felt great The battery light came on and then the ABS and DSC lights came on. Steering became difficult.

I am worried that I was full throttle and fuel was cut and the motor went lean. The car seemed to lose power up top. Idles no problem. Fires right up with jumper cables.
Old 12-08-2010, 07:54 PM
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I have the compression tester back if you need to borrow it dude

if your idle is good, what rpm is it?
Old 12-08-2010, 08:03 PM
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It idles like normal. Just a tad under 1k.
Old 12-08-2010, 09:23 PM
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Can't be hurt too bad of it idles ok
Old 12-09-2010, 12:06 AM
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I saw that MM is going to have that RX8 in MODIFIED MAG they've been tuning and building is going to be their sometime this month!!!!
Old 12-09-2010, 01:29 AM
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what rx8?
Old 12-09-2010, 01:34 AM
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Originally Posted by pdxhak
The alternator crapped out while I was full throttle.
Why are you running around at full-throttle after essentially DOUBLING your boost without verifying the tune?
Old 12-09-2010, 02:04 AM
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The RX8 modified dave has been working on that was featured in the Magazine...DONDO
Old 12-09-2010, 07:18 AM
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The engine and operating systems needs juice to function properly, plus what MM said ---> boost controller = crack pipe, if you wanna dance with the devil you better be prepared to tango in hell

Last edited by TeamRX8; 12-09-2010 at 07:21 AM.
Old 12-09-2010, 08:30 AM
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Originally Posted by MazdaManiac
Why are you running around at full-throttle after essentially DOUBLING your boost without verifying the tune?
I thought you said the tune would be safe after the actuator was adjusted and be richer up top until the final tune. I pulled off to an access road to run a data log. Great now I feel like **** again.
Old 12-10-2010, 03:44 AM
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Originally Posted by pdxhak
I thought you said the tune would be safe after the actuator was adjusted and be richer up top until the final tune. I pulled off to an access road to run a data log. Great now I feel like **** again.
Safe for the amount of boost we projected - 7 to 9 PSI, not 13.
Doubling the boost in one shot is NEVER a good idea.
Old 12-10-2010, 01:22 PM
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Originally Posted by MazdaManiac
Safe for the amount of boost we projected - 7 to 9 PSI, not 13.
Doubling the boost in one shot is NEVER a good idea.
What about mine? Cam explained how I can fix that boost fluctuation so when I do should I stay out of boost or do I need a new tune or what?
Old 12-10-2010, 01:40 PM
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You should be OK....at least good enough to run some logs carefully
Old 12-11-2010, 01:49 AM
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Originally Posted by dondo
Cam explained how I can fix that boost fluctuation
And what would that be?

Originally Posted by dondo
so when I do should I stay out of boost or do I need a new tune or what?
You should be fine, as long as you are careful.
The last time there was a Pettit fix for the bypass valve, car go boom.


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