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Pettit Super Charger Owners

Old Nov 3, 2011 | 10:24 PM
  #9251  
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From: Maryland
and another one
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Old Nov 4, 2011 | 05:16 AM
  #9252  
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From: George-uhh
Congrats moon
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Old Nov 4, 2011 | 08:13 AM
  #9253  
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awwww man--look at that little peanut head
Better be careful moon--you will fall in love with that young one.
bday nov 3nd?
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Old Nov 4, 2011 | 11:41 AM
  #9254  
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i didnt realize how beautiful the Black Halo airbox tray is until i got one--and it makes it easier to mount the a/w coolant tank.
If you dont have one --get it.
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Old Nov 4, 2011 | 05:23 PM
  #9255  
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good job moon!

Hes more of a new moon than a half moon!
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Old Nov 5, 2011 | 07:21 PM
  #9256  
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Well new front O2 sensor and still getting the same DTC P0171 code (System too lean ON 2 Fuel system).

Before I forget I also got code DTC P0507 (Idle air control system RPM higher than expected ON 2 CCM) a few days ago but it hasn't comeback since I cleared it.

It is the P0171 that keeps coming back.

This time I took the fuel pump out and cleaned everything (sock looked cleaned) and my fuel pressure is within specs.

Checked my MSD coils with a timing light. They are good.

Cleaned the TB butterfly.

Sprayed about 1/3 can of carb cleaner all over the engine bay and no idle changes (only if I sprayed at the air filter to confirm).

Took the car for a spin, full tank and various full throttle/gears/speed modes. OBDII and AEM AFR the same ranging from 11.9 to 12.1

The code shows within the first few minutes after cranking the car. I crank, it idle flutter between 900 and 1200 few times. Then to 1500 for few seconds and slowly down to 1100. After that it idles fine. (Yes, I reset the room fuse and did the pedal dance many times).

Could it be that my TB is bad or going bad?

Last edited by marsredr100; Nov 5, 2011 at 07:23 PM.
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Old Nov 6, 2011 | 08:07 AM
  #9257  
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From: macon, georgia
stop being stubborn and check the injectors, it doesnt matter that they are new
you a/f's are too high?
it sounds like the primarys may not be doing their job--since you are having idle problems?
did you spray around the w/m nozzle sites?
where on the efi log does it start showing a more lean a/f than normal?

Last edited by olddragger; Nov 6, 2011 at 08:13 AM.
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Old Nov 6, 2011 | 08:14 AM
  #9258  
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From: macon, georgia
With the space limits we have what air filter is everyone using?
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Old Nov 6, 2011 | 07:39 PM
  #9259  
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Found my problem.

It was a disconnected vacuum hose hidden behind my lower intake heat shield blanket. Somehow it came off even though it had a zip-tie. I goes to the 1/2 pipe that runs between LIM and the thermostat housing. Back on with two zip-ties and no more issues.
Attached Thumbnails Pettit Super Charger Owners-100_1671.jpg   Pettit Super Charger Owners-100_1672.jpg  
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Old Nov 7, 2011 | 05:36 AM
  #9260  
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All that for a disconnected hose
glad you found it man
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Old Nov 7, 2011 | 09:23 AM
  #9261  
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From: macon, georgia
what vacuum line is that? I dont have it. Is it the one that goes to the jet air thingy?
If so then thats the reason as I removed mine.
If you have the jet air still in there--worm clamp that bastard! It can blow off
That had to be a pretty big vacuum leak......?
Glad you found it---want to sell that new o2 sensor....? lol. I will buy it for preventive maintainance.
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Old Nov 9, 2011 | 06:24 PM
  #9262  
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Bad vac hose, bad bad bad.
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Old Nov 9, 2011 | 09:23 PM
  #9263  
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From: macon, georgia
just ordered a case of Torco fuel accelerate
Just received my set of Hawk dtc 60 pads.
Cant decide if I want to go or stop I guess?
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Old Nov 9, 2011 | 10:19 PM
  #9264  
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Order a case of crown royal I'll buy tickets to ya house.
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Old Nov 10, 2011 | 10:23 PM
  #9265  
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From: Boosted...
Originally Posted by marsredr100
Found my problem.

Somehow it came off even though it had a zip-tie.

Boost will leak if possible, in the most unlikely spot.

/that should be a Murphy sub-law.

Add some Right-Stuff to the base of the vacuum nipple, so the hose is also glued on....
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Old Nov 10, 2011 | 11:50 PM
  #9266  
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marsredr100- Thats pretty good. A 13.5 Pass @ 330hp.

My buddies El Camino with a 502 Stroke/Balanced ran 13.8 passes @ 108 mph at 500 HP/TQ... **** threw me in my seat. Im sure the feeling is similar in your ride if not more What was your speed at the end of the 1/4? Did you top out?
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Old Nov 26, 2011 | 05:42 AM
  #9267  
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had my tuning session with Steve Kan. Cam called Steve while I was there. I called him "Old man" -- like me.
We had excellent results, We left some on the table because I wanted a very conservative tune.
I guess my little LIM work payed off--as we saw something that Steve had never seen before---nor I he-he on this engine-hehehe.
We took it to 9K.
it was ambient temps of about 65F, my measure intake temp per Steve on the maf was 18C with a fan pointed toward the grill--guess my little mod on the front support beam/grill worked too hehe.
The lim runners where cool to the touch--that new bigger a/w intercooler/radiator has really worked.
with the water meth on i lost 10 rwhp and tq--i had only one 175cc nozzle post blower.
The car was NOT tuned for w/m. I will drop my nozzle size to a 60cc now --because it will be only used to he;p cool the intake charge will tracking. it is interesting that the a/f's did not change at all with the w/m on?? Go figure?
very conservative engine timing with max at 14. 14 degree split
I will get a dyno sheet posted sometime today but numbers.................
This is with the big pulley and ONLY 7 PSI BOOST.
RWHP 292
TQ 191. with TQ coming on board at 2.7K rpm
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Old Nov 26, 2011 | 06:57 AM
  #9268  
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WOW Congrats! I am Really happy for you Denny!
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Old Nov 26, 2011 | 08:19 AM
  #9269  
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From: macon, georgia
https://www.rx8club.com/attachment.p...1&d=1322317101



hope that came through ok.
interesting dyno---huh
remember this is on 7psi only

The blue line is with water meth on using one 175cc nozzle post blower
the green line is back in 2006 when we first started identifying ignition coil problems---all four of mine where very bad!
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Old Nov 26, 2011 | 08:39 AM
  #9270  
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Not opening the APV sooner was a wasted opportunity. Otherwise congrats.
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Old Nov 26, 2011 | 08:52 AM
  #9271  
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Originally Posted by olddragger
just ordered a case of Torco fuel accelerate
I would not recommend using this in a Renesis due to it's reputation for combustion deposit buildup. Premium unleaded should be fine if your fuel and timing tables are properly adjusted. If you insist on enhacing the octane level then use xylene or higher octane unleaded for dosing instead. The cheap & easy way will cost you a lot more down the road; pay me now or pay me many times more later .....
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Old Nov 26, 2011 | 09:37 AM
  #9272  
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From: Under my car
APV should have been opened at 5200 RPM.
Most boosted RX-8s make more torque that way.
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Old Nov 26, 2011 | 10:51 AM
  #9273  
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From: macon, georgia
torco will be used for track only--so it will not be that much.
i have ran toulene/xylene before just messing around with it and the car seems to like it better than the torco. You just have to carry so dang much and it is getting expensive.
I am tuned for our 93 ethanol crap
i will be bumping up my self imposed redline of 7.5K to a little over 8K.
we left some on the table--steve told me that a little over 300 was doable-- but i was happy with this at 7lbs of boost.
We played with the apv a little but just decided in the end to leave it alone. Driveability is really good. Gas milage went up a tad also
boost held steady and no belt slippage--just a good day.
Road atlanta is next w/e.
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Old Nov 27, 2011 | 09:55 AM
  #9274  
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Congrats OD!
All that work is paying off for you.
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Old Nov 27, 2011 | 01:55 PM
  #9275  
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From: George-uhh
Sounds like it all went good OD
So the tuning helped your advanced timing?

Curious to see how long you will stay with a "consevative" tune
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